I haven’t posted for a few months, I needed a break from the emotional turmoil.
In short Syvecs believe the lambda sensor issues are as a result of a leaking manifold which in turn is causing a fault with the sensor which seems feasible based on the lambda sensor wiring being replaced and knowing that the lambda sensors I have are all good.
My theory is that due to the manifold being wrapped in Thermomet it’s retained so much heat that the old Greddy manifold (which is likely 20 years old) just hasn’t been able to handle it, I’ve seen EGTs north of 900c (which is its own problem in itself). Also 20 year old super thin Japanese metal is going to struggle with the weight of a very sizeable truck turbo.
I think the lambda sensor worked fine for the initial 2-3 months as the manifold was holding up fine but ultimately it has gradually gotten worse to the point you could really audibly hear the sound of exhaust leak over what is a very noisy semi PP. Coupled with the fact you could smell the exhaust gases really strongly.
To further prove my point as to not waste money ripping off the beautiful Thermomet I invested in a smoke tester which has proven the down pipe and manifold itself were leaking.
The other issue I had been experiencing was the dashboard turning itself off randomly without any rhyme or reason. Interestingly when the car was with Syvecs they noticed a very high reading of EMI likely caused by the M&W boxes. The car is going back to Level Motorsport in November to further investigate this with a view to finding a solution.
In order to resolve the manifold issue I’ve purchased this weekend the Turblown exhaust manifold along with twin Turbosmart wastegates moving away from my big single 60mm gate. I’m told this set up offers superior flow and boost control.
I will of course need to amend my down pipe, oil feed and return as well as the TIP/TEP sensor locations and intercooler piping, all in all more investment that I wanted to avoid but with hindsight I probably should have investing in a better exhaust manifold set up at the inception of this project.
I’ve since had the new HX50 treated to the Thermomet goodness.
During troubleshooting of exhaust leaks I decided to strip the lower intake to take a look at the EGR ports to see if they were the culprit and due to the amount of reversion with the semi PP the exhaust gasket was fucked, it looked burnt in place as seen in pic.
To remedy this I did buy a new gasket from Billet Rotary in AUS but my expectation is this new paper based gasket will likely be ruined in a few months so I’ve commissioned Dobson Gaskets to custom make a gasket made with higher tensile strength, better clamping force, better chemical resistance and of course better heat resistance too. I should have the new gasket in a few weeks.
New one added last week.
Whilst I was pulling the exhaust manifold apart I noticed that one of my EGT probes was bent, again likely due to the heat. It just so happens my tuner now offer a much thicker type of probe which I’ve purchased.
If anyone is interested here is the smoke tester I purchased, it was £40 and for the money is bloody brilliant.
Next steps then are to get the new manifold fitted along with new turbo. Get all the amendments made. Ensure the lambda sensor is reading reliably, get the car tuned again on new injectors as that hasn’t happened yet. Take car to have the EMI checked in November.
2026 hopefully will bring with it a smooth and happy rotary experience. I might even finally get to run full boost with the meth squirting.
